I cannot remember the last time I took a vehicle to a mechanic other than to have tires put on and/or a 4 wheel alignment done, but after reading this thread I am somewhat worried about doing this repair. Utterly amazing that with 15,000 miles on the truck I am getting the P2285 code. Anyway, I have the correct sensor and the pigtail if I need it for a 2003 6.0 diesel, and I already had a 12 point 1 1/16" socket that fits the sensor correctly. Now, instead of cutting the socket down, can I just drop some washers in it to decrease the depth and allow the threaded portion of the sensor to protrude enough that I can screw it in? Is there another reason for cutting 3/4" off of this socket other than the fact that the sensor will slide into the socket?
In lieu of using washers in the socket, what about just putting some 3/8" rubber hose in there to prevent the sensor from sliding too far in?
Will the socket be too long to maneuver it correctly if I do not cut it down?
I am hoping to get this done from the bottom in an hour or two, but who knows. Since I started working on my Mustang 21 years ago, my motto has been to take my initial time estimate, multiply it by 3, and then that is usually the correct one. So, I'm looking forward to 3 to 6 hours on the truck this weekend. Sounds like it is going to be a blast.
Thanks to everybody that posted info on this thread. Without this thread and another one I found on another site, I would have been completely screwed.
Edit to add:
I did the repair today and went in from the top. I'm a small guy and trying to reach up from the bottom without a lift while laying on a dolly was utterly tough. I spent all of 5 minutes deciding to tackle the job from the top. I spent 4 hours on the job never having done any work in my F350's motor before and it wasn't too terrible.
For those wondering like I did about cutting down that 1 1/16" socket, cut it down. If you don't cut it down you can hardly get it in there and then it is resting against a heat shield so it is impossible to get the swivel onto the socket. Best destruction of a good socket I have ever had, and definitely worth the cost of a new socket to replace it. The most frustrating part for me was trying to get the pigtail back on the ICP Sensor because the tab was 180 degrees from where it had been on the bad sensor and trying to line everything up and then push the plug in was very tough. Otherwise, a lot of time just spent moving parts out of the way to get to the ICP sensor.
After replacing it, the truck runs smoother and it has a ton more power. It pulls really well when accelerating now.
Again, thanks to everybody that posted to this thread. I was coming in and out of the house while doing the repair so I could read this thread and look at the pics.
In lieu of using washers in the socket, what about just putting some 3/8" rubber hose in there to prevent the sensor from sliding too far in?
Will the socket be too long to maneuver it correctly if I do not cut it down?
I am hoping to get this done from the bottom in an hour or two, but who knows. Since I started working on my Mustang 21 years ago, my motto has been to take my initial time estimate, multiply it by 3, and then that is usually the correct one. So, I'm looking forward to 3 to 6 hours on the truck this weekend. Sounds like it is going to be a blast.
Thanks to everybody that posted info on this thread. Without this thread and another one I found on another site, I would have been completely screwed.
Edit to add:
I did the repair today and went in from the top. I'm a small guy and trying to reach up from the bottom without a lift while laying on a dolly was utterly tough. I spent all of 5 minutes deciding to tackle the job from the top. I spent 4 hours on the job never having done any work in my F350's motor before and it wasn't too terrible.
For those wondering like I did about cutting down that 1 1/16" socket, cut it down. If you don't cut it down you can hardly get it in there and then it is resting against a heat shield so it is impossible to get the swivel onto the socket. Best destruction of a good socket I have ever had, and definitely worth the cost of a new socket to replace it. The most frustrating part for me was trying to get the pigtail back on the ICP Sensor because the tab was 180 degrees from where it had been on the bad sensor and trying to line everything up and then push the plug in was very tough. Otherwise, a lot of time just spent moving parts out of the way to get to the ICP sensor.
After replacing it, the truck runs smoother and it has a ton more power. It pulls really well when accelerating now.
Again, thanks to everybody that posted to this thread. I was coming in and out of the house while doing the repair so I could read this thread and look at the pics.